BP, Halliburton knew well cement was ‘unstable’
BP, Halliburton knew well cement was ‘unstable’ BP and Transocean, another partner, ‘misinterpreted or chose not to conduct’ key tests, it adds
Following the explosion that killed 11 workers and triggered the massive Gulf oil spill, the Deepwater Horizon drilling rig burned for two days before sinking.
BP and its cement contractor, Halliburton, knew weeks before the Deepwater Horizon explosion that the cement mixture they planned to use to seal the new well was unstable but still completed the work, staff for the presidential commission investigating the accident said in a letter Thursday.
That improper cement work “may have contributed to the blowout” on April 20 that killed 11 workers and led to the largest offshore oil spill in history, the staff stated in the first official finding of responsibility for the disaster
BP knew well cement was ‘unstable’
BP and its cement contractor knew weeks before the Deepwater Horizon explosion that the cement mixture they planned to use to seal the new well was unstable, investigators said.
Other factors have also been cited as possibly contributing to the explosion, among them a faulty blowout preventer and BP’s decisions to use fewer stability rings on the well piping and seawater instead of heavier mud to plug the well until it was to be used for production.
The staff noted, however, that had the cement done its job it would “have prevented hydrocarbons from entering the well” and triggering the explosion.
The commission staff said that “Halliburton and BP both had results in March showing that a very similar foam slurry design to the one actually pumped at the Macondo well would be unstable, but neither acted upon that data.”
Commission staff also cited Transocean, the owner of the drilling rig, as sharing some blame.
“The oil industry has developed tests, such as the negative pressure test and cement evaluation logs, to identify cementing failures” the team said, but “BP and/or Transocean personnel misinterpreted or chose not to conduct such tests at the Macondo well.”
The letter also stated that independent testing of the type of cement used by Halliburton showed it was not stable.
“Halliburton (and perhaps BP) should have considered redesigning the foam slurry before pumping it at the Macondo well,” the investigators added.
BP, as part of its own internal investigation, also conducted tests that showed the cement mix was flawed, but its analysis was criticized by Halliburton, which said it was not the correct formula.
By contrast, the commission obtained proprietary additives from Halliburton as well as a recipe to recreate the slurry that was used on the well.
A spokeswoman for Halliburton said the company was reviewing the findings and would have a response later Thursday. Halliburton has said tests showed the cement mix was stable.
Two of those tests were conducted in February, and two more in April.
The staff said the results from one February test were sent to BP on March 8 “in a technical report along with other information. There is no indication that Halliburton highlighted to BP the significance of the foam stability data or that BP personnel raised any questions about it. There is no indication that Halliburton provided the data from the other February test to BP.”
For the last test, the staff wrote, “Halliburton personnel again modified the testing procedure, and this time — for the first time — the data indicated the foam slurry design would be stable. We are not yet certain when Halliburton reported this data internally or whether the test was even complete prior to the time the cement job was poured at the Macondo well. Halliburton reported this data to BP after the blowout.”
A BP spokesman had no immediate reaction.